A New Way's New Home
Group effort brings a beautiful engine back to life
August 2006
By Christopher Markley
Having bought several smaller engines, I
decided I wanted something physically bigger to play with. I had
seen several New Ways in magazines and on the Internet, but never
in person. Liking the painted detail and the air-cooled design, I
began looking on the Internet for a project.
RELATED CONTENT
Rod and piston assembly, Sharpies, Maytag fuel mixture, spray cart and Easy Engine...
It was a half-stroke like the Lenoir...
Bill Cherry, a co-worker and I used a porta power pump to remove a Maytag...
The Sterling crankless high-speed engine may forecast a revolutionary trend in design...
The engine shows in the Michigan area as well as the show in Portland...
In Kansas, eBay presented a nice option: a Type C, 4-1/2 HP,
double-flywheel with a stuck piston and several missing parts.
After several e-mail conversations with the seller, Tim Christoff,
I won the bid and picked up the engine in the fall of 2002. Tim
helped my brother and I load it into the truck, then he showed us
some of his projects, and gave us photos and drawings of parts I
would need for this engine.
Tim had gotten the engine from Terry Ward of West Virginia.
Terry said the engine had been hooked to a line shaft on a farm
when he found it. The flywheel on the governor side was moved out
1/2-inch and a lead washer of that thickness was placed on the
shaft to compensate for the move. Also, while the wheel was off,
somebody cut a hole in the leather top of a boot and placed this on
the main shaft. I am not sure of the reason for this addition. The
engine is also missing the original tag, but Terry believes he has
it and is looking for it.
We took the engine home, and the next morning I started looking
it over better. I could see the piston was stuck about halfway, and
it looked like there were leaves and other gunk in the cylinder. I
got the Shop Vac out and blew air up in the cylinder. When I looked
up again, I thought I saw light. I ran a string of Christmas lights
through the spark plug hole and could see a wedge-shaped hole in
the top of the piston. A few light taps of a wooden dowel rod
brought down the rest of the piston top.
Hmm … a convertible piston. I figure at some point somebody had
tried to use a rod and hammer to get the piston free, but it didn't
go right. I contacted Tim about this and he started looking for a
way to help me out.
The top of the piston was done for, but there was the
possibility of welding a new top on, so I wanted the rest of the
piston out in one piece. I tried several methods of freeing up the
piston. Five months of electrolysis did nothing. I also used heat,
dry ice and PB plaster. Nothing. After two years, I was ready for
the mother of all pulleys.
Page: 1 |
2 |
3 |
Next >>